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We found the following complaints for NEWMAR DUTCH STAR (1999)

Read complaints for NEWMAR DUTCH STAR (1999)


While driving long distance vehicle stalled unexpectedly, losing all power steering and brakes, which could have causeda crash.took to dealer. Dealer said it was due to the fuel filter.however, this problem occurred 12 times, and replacedfuel filter 10 times, butproblem was reoccurring.the motor stops running while under motion when water gets in the fuel filter causing brake and steering loss.it takes only a teaspoon of water to clog this filter.

Driving on i-90in some rainy weather, error code light came on. I stopped checked all fluid levels & continued on. A few hours later theengine began to increase in speed on its own .rpm's were at 2000 & the coach was almost impossible to stop.the chassis connector ( connects coach to engine and electronic control module) filled with water and caused shorts,crosses,and grounds in the wiring and caused the motorhome to increase in speed on its own. The brakes were hot and smoking when we finally got stopped.technician pulled connector apart, used compressed air to remove the water & a contact cleaner to clean the probes & contacts in the connector. Connector was plugged back together, all shorts, grounds, and crosses were gone.technician cleared all error codes, put silicone on connector to keep water out until connector can be replaced. Upon leaving the shop transmission would not shift up until rpm's were at 2000. It will not shift into 6th unless it is done manually.

The contact owns a 1999 newmar dutch star.the contact took the vehicle to the service center for regular preventive maintenance, and also because he noticed the shut off switch for the electrical systemmalfunctioned.the service center stated that a fire previously occurred because the wiring melted.the contact did not smell anything burning nor did he see any flames.he didnot know when the fire occurred.the current and failure mileages were 70,000.the consumer stated the damage was located at the rear compartment. Updated 05/21/07.

While on a downgrade with the engine brake engaged and in 4th gear, at about 1900 rpm, the side mounted fan exploded sending plastic and metal parts out the rear of the motorhome showering the vehicle being towed and another vehicle following behind. Upon inspection the fan, which is driven by a hydraulic pump, was supposed to be attached by two bolts to a cross bar between the radiator and the engine. The bolt holes in the hydraulic pump were elongated and both bolts had sheared off allowing the pump to fall down which resulted in the fan blades hitting the chassis frame and causing the fan to bounce around the compartment hitting the radiator and piping and the intercooler piping. This hydraulic system is also part of the power steering system. Upon being towed back to rapid city, sd there was another dutchstar (a 2000) at the freightliner dealer with the same failure. Replacement parts consisted of a hydraulic drive motor, radiator and intercooler plus all the replacement fluids for both. I retained the hydraulic drive motor if needed. If the fan had severed the hydraulic line that would have disabled the steering system with loss of the ability to steer. Also if there were not a vehicle being towed that took the blow of most of the parts coming off the engine the vehicle being driven and following behind could have received significant damage and possible resulted in an accident.

The dragging tail pipe had been pulled from the muffler, breaking the weld for the tail pipe attachment.(nar)*ph

Dt*: the contact stated while driving 50 mph on wet roads in the rain, moisture was picked up through the intake manifold.the vehicle partially lost power, but kept moving.the vehicle was not seen by a dealer.prior to this incident, the air intake tube had been replaced by a service dealer due to the same issue, but the problems persisted.the manufacturer was contacted, who stated that the contact had the most up to date fix for this problem, and that it should not have recurred a second time.

Newmar corp are were using inferior aftermarket headlamps on dutchstar motor homes in the years 1999,2000 and possibly other years . Unable to see te road after dark.

Had bad fuel leak caused by use of ultra low sulfer diesel fuel.(uldf).replaced fuel transfer (lift) pump p/n 4935007old pumpwas available.

While driving long distance vehicle stalled unexpectedly, losing all power steering and brakes, which could have causeda crash.took to dealer. Dealer said it was due to the fuel filter.however, this problem occurred 12 times, and replacedfuel filter 10 times, butproblem was reoccurring.the motor stops running while under motion when water gets in the fuel filter causing brake and steering loss.it takes only a teaspoon of water to clog this filter.

The 21ft awning on the right side of the coach accidentally deployed while driving at 65mph. Luckily i was in the right hand lane of a 4 lane divided highway so it didn't hit any other cars. It was stowed as per the manufacturers instructions and apparently came loose in some gusty crosswinds. Several other rv owners have had a similar problem with this awning(a&e 9000 by dometic corp).

Front wheel bearings failure. While driving motorhomestopped completely because of front wheel bearing failure. The front wheel bearingshave been replaced three times.first replacement in oct of 99. The next replacements were in2 weeks later.problem was reported to the manufacturer. As of 01/07/ 2000 right front bearing fluid still not up to full capacity.

Recall 04v037000 concerning newmar tires. Dealer was unable to honor recall because no part was available since july 31, 2004.

Left front tire blew out. Tire on the rear dual wheel also blew out.tires totally disintegrated.motor home was damaged by tires.a third tire also exploded (michelin 255/80r 2215), consumer replaced with another tire brand.

Dot d6h6ak3x159 255 80r22.5 xrv consumer states that the right front tire blew at 55 mph. Right rear tire blew.please provide any further information.mr

Both front windshields worked themselves out of the rubber gasket around the windshields. Consumer has a concern that the windshields may not stay properly in place while driving at high speed and/or in inclement conditions. Manufacturer was notified. The rv was taken to a glass company who indicated that the glass was too large for the opening and refuse to attempt repair.another glass company stated that the curvature of the glass didn't match the curvature of the body.they also refused to repair the glass.the manufacturer will only perform no warranty work at the plant during winter months (jan, feb, march).the consumer believes this problem is a design flaw.

Front windshield shattered on two occasions by rolling onto a minor dip inroad while detouring. Dealer andmanufacturer have been notified. Feel free to provide any further information.

Right front wheel bearing failed after manufacturer recall work performed. Mjs




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