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We found the following complaints for FORD THUNDERBIRD (1992)

Read complaints for FORD THUNDERBIRD (1992)


Driving home in left lane, street lights not bright, another vehicle in left lane not moving, no hazards or other lights, thunderbird rearended vehicle, air bags did not deploy.

Coming across a small bridge that was iced, lost control, hitting the guardrail, totally demolishing the front.neither dual air bags deployed at any time even after being towed to body shop.please describe details.

Electrical system shorted out causing lights to go on and off continuously.

Vehicle was parked for 20-25 minutes whena defective alternator, caused a fire in the engine compartment area. Dealer has been notified.

Vehicle experienced failure of the recall component (96v-071) prior to recall notice, resulting in fire. *mjs

Consumer' s vehicle experienced the same problems as stated innhtsa recalls 96v071000and 99v27500 concerningignition system andheadlights. The dealership indicated consumer's vehicle not included in the recall due to vin.

Recall 96v-071 (ford 95s28) was originally repaired on 12/2/97. Vehicle is now experiencing a similar problem. Dealer will not honor recall repair, and consumer is beng charged for expense of installing another new ignition switch.

96v071000; recall work was done by koons ford, falls church, va. The consumer was driving and the steering column wires melted and smoldered, the consumer is not satisfied with the work done prior to the incident. Currently the dealer cannot duplicate the problem.

Nhtsa recall 96v071000 and manufacturer's recall 95s28/ ignition system failure. Had recall done on may 26,1999, and remedy failed.owner replaced the part himself, ignition switch was found separated from the mounting harware.contacted ford about the problem, but they showed no concern.*ml

Vehicle exhibits symptoms similar to earlier models with tfi; sudden stall at any speed or configuration.always associated with high ambient/enginetemperature.problem has occured on highway, creating extraordinarily dangerous situation. Dealer technician dismissed possible ignition failure when asked.

Sometimesturn signal works and sometimes they do not work.consumer has to wiggle key, and signals may or may not illuminate.causeunknown. Recall 96 v 071 000 described the same problem. Please provide any further information.

Ignition module malfunctioned.ford cannot provide part, stopped producing the part.

Whilevehiclewas being driven a malfunction occurred withinignition module,causingvehicle to completely shutdown.please give any further details.

Vehicle experienced sudden acceleration which damaged engine due to failure of the computer unit.

Vehicle was parked, under the interior compartment, under the dash, electrical short.

Consumer was driving and smoke came from the ignition ( steering column ) . Please describe .

Electrical short in the ignition switch, causing the vehicle to catch on fire in the steering column.

While placing the key in the ignition switch vehiclefailed to start.consumerturned off the vehicle, and then restarted it.drove it to the dealer for inspection, and mechanic replaced solenoidswitch inside the ignition due to a burnt out wire.

While placing the key inside of the ignition switch the key failed to come out from the ignition. Consumer had the vehicle towed to the dealer for inspection, and mechanicdetermined that the ignition switch needed to be replaced.

Brakes: brakes has beenreplaced three times within three years. Brakes vibrate and wear out within a year. Had new brake pads installed and rotors turned. Also vehicle caught fire on the left side 3-2-97. Probable cause electrical. Recall 96v071.

In the u.s. Military stationed in europe. Fuel pump and relay malfunctioned. While installing new fuel pump and relay, the ford technician found the wiring harness providing current to the pump was improperly installed or was a faulty design. It had chaffed through the harness casing exposing the charred and melted wires inside. Subsequent chaffing of inner wires caused a short in the circuit and melting of the wires themselves. Due to the proximity of the short, an explosion could occur if fuel vapors are present.the technician was surprised it had not exploded. This vehicle has a current recall for other fuel system defects.a combination of the 2 could be deadly if the owner in unaware of either problem area. I have and will retain the harness for further investigation if needed.

The harness at the alternator has caught fire twice and i have replaced the alternator three times in two years. This is a very dangerous situation. It starts smoking and suet comes out and you think the car is going to blow up. It is a very frightening experience. The mechanic found service bullentin article #96-21-4 which describes this. It has happened to me twice in less than two years. I am very distrubed. Please help me.

While driving vehicle at 40mph at night,headlights would go out. Would not have any warning. The headlights were repaired at least 3 different times for the electrical problem. (rq 98015).

While driving down the road at nightheadlights will just go out. Consumer had a recall on the headlights. Took vehicle to dealer , and they replaced headlight switch and some other wires. About two weeks later, the same problem returned.

While driving the eec fuse blew out and caused the vehicle to stall.the dealer was notified. *nlm

Headlights goe out for various intervalswhich may be preceded by flickering or blinkingas aresult ofcircuit breaker opening. Dealer has been notified. Please provide further information.

Electricial fire in the steering column of the dash board, resulting in a bad fire.

While driving consumer smelled smoke coming in from the vents. Consumer pulled over, lifted the hood up, and vehicle caught on fire.consumer was able to extinguish the fire. Consumer had the vehicle towed to the dealer for inspection.

The day after having the water pump replaced after a failure, the engine temperature raised to the maximum that the gauge can display (no specific temp, just c-normal-h).took car back to the garage where the water pump was replaced and they said that the head gaskets had blown and repair would cost $1100.for a second opinion i limped it to a person who "secializes" in super coupes and he confirmed the diagnosis.he said he had seen many tbird sc's come in with the same problem and milage did not play a part in the defect.he reported to me that the main malfunction was not only a poor quality gasket, but that the heads were machined to too high of a tolerance.the heads were machined, the gaskets replaced, etc etc, to the tune of $1000.

Coolant is put into overflow bottle and is not pulled back into engine in a timely manner. Engine develops an air bubble and quits running.

The radiator in the vehicle melted at 51,000 miles.

While driving vehicle made a popping noise, then smoke came out of exhaust caused by a blown out had gasket.

Vehicle in dealer shop forrecall repairs. Dealer informed consumer that there was a blownengine head gasket.

Filled vehicle with fuel & drove home. Parked vehicle in garage. Noticed an odor of gasoline. Checked vehicle & discovered a leak underneath vehicle. Took vehicle to mechanic & the gaskets were replaced, twice. The problem still exists. Took vehicle to dealer & mechanic would not check unless a diagnostic test was done.

Driving at 40 mph and engine stopped. Got out look to see the head gasket was blown.

Head gasket failed causing vehicle to stall in traffic.

Failed headgaskets while vehicle was strapped to chassis dynomometer.failure happened at 3000rpms.head gasket failure caused the top plastic radiator tank to explode with many witnesses.

Seems to be a defect in all ford thunderbird sc headgaskets.factory mill is incorrect and not done very well.recall is necessary to have ford fix an issue that has been recalled for the 1994/95 models.ford should recall the 1989-1993 sc, same drivetrain.

Head gasket-car began skipping and then white smoke came out of exhuast.i drove it home (3 miles).i pulled the spark plugs and found that the number 3 cylinder plug clean and wet.i did some research and found this to be a common problem with this motor and cylinder.why won't ford help?i have yet to bring it to a garage so i don't know if the head or block is damaged.i am hoping not!transmission-aod modelstarting at about 79,000 miles it began to shift funny and got progressively worse as time went on.now shifting eratic, was looking into fixing it when the head gasket problem came up!!!!!

While driving at 40 mph vehicle started smoking. Consumer pulled over and noticed engine head gasket blew out.

Head gasket blew resulting in complete engine failure when the cylinders filled with coolant fluid.yh

When a service employee started vehicle and moved it into garagewhite smokecame out ofvehicle.upon examination bydealership, engine head gaskethad blown, and motor needed to be replaced.consumer paid approximately $4175.00 to have this defect repaired.

Premature failure of the 3.8l engine head gasket.

Head gaskets failed. Yh

Premature failure of the 3.8l engine head gasket.

Ford motor co. Has recalled many 3.8l v6 because of head gasket. When i called them they were only recalling fwd cars. I called three different dealers stevens ford, park city ford, and miller ford they all told me they would use the same kit ( bolts and gaskets) called out in the recall. I think that ford should stand behind there product and recall all 3.8l v6's with this problem. Please let me know? thanks joe.

Premature head gasket failure - repair cost of $970.

The day after having the water pump replaced after a failure, the engine temperature raised to the maximum that the gauge can display (no specific temp, just c-normal-h).took car back to the garage where the water pump was replaced and they said that the head gaskets had blown and repair would cost $1100.for a second opinion i limped it to a person who "secializes" in super coupes and he confirmed the diagnosis.he said he had seen many tbird sc's come in with the same problem and milage did not play a part in the defect.he reported to me that the main malfunction was not only a poor quality gasket, but that the heads were machined to too high of a tolerance.the heads were machined, the gaskets replaced, etc etc, to the tune of $1000.

Engine head gasket has been leaking for a while and finally went. Heard numerous reports and read articals ranging from a show by 'motor trend ' to dealer comments on the problem with defective head gaskets in 3.8l engines. Also, knownumerous people with an engine like mine ,have experiencedthe same problem.the "light bar" inside the taillights areanother problem, you don't see a t-bird on the road today that doesn'thave at least part of their tail lights burned out so i know its not just mine and they started doing this many miles ago!i take good care of my vehicles,so i know this is not from abuse! like i saidwhen dealers tell you they're having a problem with certain parts and car shows,magazines , and consumer reports say there is something wrong with ahead gasket on a certain engine you know you're not alone!replacing a head gasket is an expensive repair , i thought i would check into this before footing the bill myself. Please let me know as soon as you can if anything can be done about this as i'm not able to drive the car ...thanks ,lynn.

The vehicle overheated and would not start after it had been turned off.once it did get started it was blowing smoke from the exhaust. .it has not ran since then due to the information from the dealer on the faulty head gaskets.

After having vehicle serviced it stalled.vehicle was towed back to dealer . Technician stated that head gasket was blown.the engine failed while the vehicle was undergoing inspection maintenance.

Left and right outer and inner rockers rotted. Bad design, no ventilation built in to dry moisture inside rocker. Therefore they rot till there is no more rocker, costing $700 per side to have a ford body shop to cut out and weld in new rockers.

Engine missing. Water in cylinder. Head cracked/gasket blown. Dealer will do nothing for there is no recall but states this engine has a reputation for cracking heads. States 94-95 models recalled heads but not '92. Dealer unable to get replacement head. States newly designed head won't be released until mid summer and cannot get the part to fix my car.3 repair shops repeated "those are bad to crack heads" and are unable to get replacements.parts stores are unable to get this head. Manufacturer stated with no recall, they will do nothing. Stated they have no access to parts information... This is obviously a known problem but ford will not acknowledge it.i have a broken car and no way to fix it.

No summary listed for above vehicle.

Electrical fire under the hood.

After having vehicle serviced it stalled.vehicle was towed back to dealer . Technician stated that head gasket was blown.the engine failed while the vehicle was undergoing inspection maintenance.

The orginal speedometer was replaced at 7,000 miles, the second one was replaced at 5,000 miles and the third one at 8,000 miles.please describe further details. The needle will not program past 38 mph also heater not working properly low heat and also a/c low..

Rear upper brake light: it contians two bulbs one of them was broken and the holder was melted and burnt. Didn't cause any damage except for the connector. Not sure on date just noticed when i noticed the light wasn't working.

Componant: upper mounted taillightrepeated stop and go traffic created excessvie heat in the unvented plastic mounting. Plastic melted and driped onto bulbs causing them to fail. Possibility of fire.

The brakes switch goes out,consumer loses brakes lights,no cruise control and is unable to shift from parkinto drive. The switch has been replaced (6) time since owning vehicle in july 92.

Vehiclewas not equipped with fog lights. Also, headlight switch malfunctioned,causingheadlights to flicker on and off, affecting driver's visibility and may result ina crash.dealer replacedmulti-functionswitch which did not correct the problem. Vehiclewas not included inrecall 99v275000 although it had the same problem.vehicle was repaired.*ml

When using the fog lights they flash on and off everytime headlamps are changed, problem occurs regularly.

When fog lights are on the headlights go out and won't come back on immediately.the headlight switch has been replaced, but this problem still occurs.ford says the recall time has expired and they are no longer obligated to fix this problem.recall was dated 1999 and only the switch was replaced.i payed for the repair before the recall and was told that the problem had already been taken care of.i am afraid of crashing causing injury because of this, because you don't know when head light failure will occur.

While drivingheadlights flicked off and on which caused poor driver's visibility. Also,recall99v275000dealt withsame type of problembut this vehicle wasnotincluded in recall due to vin.please provide any further details.

While driving headlights go off and come back on, appointment with dealer.

While driving headlights go off and come back on, appointment with dealer.

My headlights turned off and turned back on.they do this all the time.

When driving headlights turn off and/or flicker without prior warning, causing poor driver visbility.also,recall 99v275000 deals with the same problem.however, this vehicle is not included due to vin.please provide any further details.

When driving the vehicle at night, the headlights would work intermittently. The consumer has made contact with the dealer. Please provide any further details.*ph

Wiring for the headlights contains too much current causing flickering of lighting due to design. Mjs

Recall headlights does not examine 4-prong connector to multi-function switch (headlamps).connector casing completely burned through; 1/2 inch outer edge, 3/16 inch inner edge, with signs of burning and melting multi-function casing inner and outer next to switch assembly ignition causing insufficient operation of headlights.fog lamps used at all times during operation of headlamps.possibility of fire?!headlights flicker/shutoff with operation of fog lamps but return to normal once fog lamps shutdown, even with damage to connector.dealership service assumed multi-function defective but would not acknowledge and/or examine the possibility of electrical problem associated with headlamp switch.dealer did not notify owner of electrical problem.dealer and manufacturer notified and do not see this as a "safety issue" nor acknowledge any responsibility since not covered in original recall and vehicle not covered by warranty.(via first class mail:pictures)

Headlights work intermittently. *sd

While driving at night with headlights on,headlights will flick. Then, will go out completely.recall issued for the 93 model for this same problem, but not 92.dealer says there is nothing they can do.*ml

Recall # 99v275000 ford/headlights; after recall was performed owner was driving and the headlights went out.dealer was contacted.after charging $55.00,dealer stated that problem was not related to the recall, even though this problem had to do with the wiring as well. Problem has not been corrected.*ml

Consumer' s vehicle experienced the same problems as stated innhtsa recalls 96v071000and 99v27500 concerningignition system andheadlights. The dealership indicated consumer's vehicle not included in the recall due to vin.

While driving the headlights go out.please describe.tt

While drivingheadlights go off unknowngly. Sometimes the headlights will come back on within a few seconds and sometimes they do not.there has been 3 different repairs done to the headlights, which have not done any good. When contacting ford customer service, owner was informed that vehicle was not included in recall 99v275000 ford/headlights due to vin. Please provide any further information.

On 12-14-1999 the headlight switch on my 1992 thunderbird was replaced under recall number 99s30.the original switch had exhibited the symptoms listed in the recall letter i received (i.e. Headlights flickering offwhen the fog lamps were used).i am now beginning to see similar symptoms with the switch that was installed last year by the ford dealer.this morning when leaving for work i pulled the light switch out fully and had no headlights.i inspected the condition of the headlight fuse and found it to be good.i then tried wiggling the switch while in the on position (that had worked with the original switch) and the lights eventually did come on.since then i turned the lights on and off several times without a failure.i contacted the dealer that did the recall work last year and ford's customer service dept., and was told by representatives from both that there is no warranty on parts replaced under a recall and that, therefore, i would have to pay the cost of replacing the switch myself.i will be replacing the switch in the next day or two, and will retain the receipt for reimbursement in the event there is another recall related to the switch.i am very disappointed that ford is not willing to replace the switch.apparently they are not under a mandate to do so, but they could if they wanted to in the name of "customer satisfaction".they know as well as i do that the switch should last a lot longer than one year.

While driving at night headlamps go out without prior warning due to wiring harness chaffing against radiator supports. Dealer twice attempted to correct it. Tt

While driving at night the headlights intermittently shut off or flicker on and off, reducing visibility for the driver.the dealership has not examined the vehicle to determine the cause of the problem and informed consumer that the vehicle was not affected by recall campaign 99v275000.*nlm

While driving headlights go off and come back on, appointment with dealer.

Recall 99v275 000/headlights: headlights intermittently would go out for various intervals which wasproceeded by blinking or flickering.this caused loss of visibility. Dealer notified and informed consumer that vehicle was not under recall due to vin.

Headlamps flicker on and off as described in nhtsa's recall campaign id #99v275000.the 1992 ford thunderbird was manufactured in the period covered by the recall period.checking with ford motor company resulted in their saying the vehicle is not covered by that recall.repeated requests to conider this issue similar to that recall were denied.i would like to suggest that the recall did not cover enough vehicles.

The headlights started flickering after ignition switch was recalled and replaced.i was traveling from a funeral when the lights started while on the interstate at around 2300 hrs.

No summary listed for above vehicle.

The contact owns a 1992 ford thunderbird.in april of 2000, the contact received a recall notice regarding the headlights.the recall repair was not performed at that time because there were no failures with the vehicle.currently, the headlights and fog lights flicker on and off and two parts need to be replaced.she took the vehicle to the dealer and they advised her to call ford motor company.the manufacturer was unable to provide any assistance.the recall number was unknown.the current and failure mileages were 58,800.

Dimmer switch shorts, causing headlights to go out. *dsh

While driving 55 mph with lights on, they would flicker on & off. Problem started w/high beams & then w/low beams; eventually went out completely; pulled over & cooled vehicle down. Lights worked afterwards. Had changed same identical switch 7 years ago.

When driving on highway headlights went out. Pulled over & turned off switch & then back on, headlights appeared. Would last about 30-40 seconds. Happens interminttently. Took to dealer & mechanic said light switch overheated. It effected headlights.

The headlight switch gets heated and cuts the headlights off.

Head lights went out several times causing poor visibility due to failure of the head light switch.

The auto lamp on/off delay system randomly turns of my headlights at night even when the delay system is turned off.

Vehiclewas not equipped with fog lights. Also, headlight switch malfunctioned,causingheadlights to flicker on and off, affecting driver's visibility and may result ina crash.dealer replacedmulti-functionswitch which did not correct the problem. Vehiclewas not included inrecall 99v275000 although it had the same problem.vehicle was repaired.*ml

When fog lights are on the headlights go out and won't come back on immediately.the headlight switch has been replaced, but this problem still occurs.ford says the recall time has expired and they are no longer obligated to fix this problem.recall was dated 1999 and only the switch was replaced.i payed for the repair before the recall and was told that the problem had already been taken care of.i am afraid of crashing causing injury because of this, because you don't know when head light failure will occur.

Head light switch failed prior to recall noitce 99v-275 consumer wanted to be reimbursed for repair.nlm

Nhtsa recall no:99v275000 and manufacturer's recall no:99s30 concerning headlights.no parts were available, and dealer didn't say when they will be available.

Vehicle experienced failure of the recall component prior to recall notification (99v-275). *mjs

Engine head gasket has been leaking for a while and finally went. Heard numerous reports and read articals ranging from a show by 'motor trend ' to dealer comments on the problem with defective head gaskets in 3.8l engines. Also, knownumerous people with an engine like mine ,have experiencedthe same problem.the "light bar" inside the taillights areanother problem, you don't see a t-bird on the road today that doesn'thave at least part of their tail lights burned out so i know its not just mine and they started doing this many miles ago!i take good care of my vehicles,so i know this is not from abuse! like i saidwhen dealers tell you they're having a problem with certain parts and car shows,magazines , and consumer reports say there is something wrong with ahead gasket on a certain engine you know you're not alone!replacing a head gasket is an expensive repair , i thought i would check into this before footing the bill myself. Please let me know as soon as you can if anything can be done about this as i'm not able to drive the car ...thanks ,lynn.

Sometimesturn signal works and sometimes they do not work.consumer has to wiggle key, and signals may or may not illuminate.causeunknown. Recall 96 v 071 000 described the same problem. Please provide any further information.

Vehiclewas not equipped with fog lights. Also, headlight switch malfunctioned,causingheadlights to flicker on and off, affecting driver's visibility and may result ina crash.dealer replacedmulti-functionswitch which did not correct the problem. Vehiclewas not included inrecall 99v275000 although it had the same problem.vehicle was repaired.*ml

Multi-function switch failed.nlm

Smells gas fumes really bad but not at all times. Problem looked at but no leaks found. Please describe details.tt

While traveling on the highway, the consumer had smelled gasoline coming inside of the vehicle.dealership is aware of the problem.(*scc

When the car is stopped at a red light or down below a half a tank the driver smells gas odor.

Ea95-030; several fuel components replaced resulting leakage, fumes and erratic failure of vehicle performance would stall. Please describe details.tt

When the car is stopped at a red light or down below a half a tank the driver smells gas odor.

Fuel leaked from fuel tank area, emitting strong fumes in garage.

Gas line goes over rear axle & doesn't have rubber padding. Hole was created by rubbing, causing fuel leak which blows back onto tailpipe & muffler. Took to garage & then dealer & nothing was done.

Fuel line had been replaced 2 years ago under recall, now ford says won't cover twice.

Black plastic bends rubbing/chaffing,wearing holes in fuel line.*sd

Service shop stated that a hole developed in the fuel line, caused by the fuel line rubbing against the frame of the car.

Fuel gauge became erratic, suddenly dropping from full to empty after the sender was installed, second installment was a ab sender unit and pump assembly.

In the u.s. Military stationed in europe. Fuel pump and relay malfunctioned. While installing new fuel pump and relay, the ford technician found the wiring harness providing current to the pump was improperly installed or was a faulty design. It had chaffed through the harness casing exposing the charred and melted wires inside. Subsequent chaffing of inner wires caused a short in the circuit and melting of the wires themselves. Due to the proximity of the short, an explosion could occur if fuel vapors are present.the technician was surprised it had not exploded. This vehicle has a current recall for other fuel system defects.a combination of the 2 could be deadly if the owner in unaware of either problem area. I have and will retain the harness for further investigation if needed.

Noticed gasolene odor in interior, found one of three plastic fuel line hoses had worn hole into from rubbing against body, causing gas to soak into carpet.

Fuel line is leaking prior to recall (97v-159). Yh

Recalls 97s84/ 97v159000 were received on5/97, and dealer and manufacturer were contacted. The dealer has not responded to consumerr's call/request for remedy of recall. Last time comsumer tried to contact dealer was in 10//97.

Fuel line has worn through where the bracket are located near the fuel tank.tt

Fuel line protruded below the frame of the vehicle after recall repairs(97v-159).

1)1992 ford thunderbird vin [xxx], fuel line chaffed against floor pan causing a pin hole resulting in fuel leakage (exactly as in nhsa id: 97v159000 issued 09/17/1997).2) fuel line leaked strong odor and exteam fire danger.3)john's repair 189 e. 2nd s. Soda springs, id replaced fuel line 10/20/03 $292.66.contacted ford at 800-392-3673, 07/28/2004, they stated this vin had no outstanding recalls, they couldn't cross check nhtsa id # to ford's recall number and ford wouldn't reimburse me for repair.updated 07/25/2012information redacted pursuant to the freedom of information act (foia), 5 u.s.c. 552(b)(6)

Vehicle was repaired per a recall involving the fuel line.now fuel line hangs below the frame of the vehicle.

See campaign id 97v159000.campaign describes exact problem encountered, but does not apply to my specific car.problem: nylon fuel line at gas tank chafed to create fuel leak.

The way the gas line is routed to the tank it leaks gas and could cause a fire hazard.

Filled vehicle with fuel & drove home. Parked vehicle in garage. Noticed an odor of gasoline. Checked vehicle & discovered a leak underneath vehicle. Took vehicle to mechanic & the gaskets were replaced, twice. The problem still exists. Took vehicle to dealer & mechanic would not check unless a diagnostic test was done.

Fuel leak,fuel tank assembly, the plastic line rubbing against the frame, metal drops , also fumes come inside of vehicle.

Recall repair work completed on the fuel lines however did not rectify leakage, faulty sender and pump assembly in the fuel tank failed also.

Fuel lines failed prior to recall notice causing fumes and leaking.

Fuel line leaks at gas tank.

The doors have been a problem for quite a few years, they seem to be too heavy for the hinges as they sag and require us to lift the door to get them to shut.the front seat automatic seat belts don't work properly at all as they do not know when to retract and passenger side stays at bottom of track and shutters all the time.the parking brake pedal does not stay elevated, which causes the in-dash brake light to come on during operation.

The emergency parking brake will not engage when it is applied because of awratchet problem.

Parked in driveway in park brake set and vehicle rolled back.

The plastic transmission cable end broke off the throttle body causing the gas pedal sticking to the floor.*et

The orginal speedometer was replaced at 7,000 miles, the second one was replaced at 5,000 miles and the third one at 8,000 miles.please describe further details. The needle will not program past 38 mph also heater not working properly low heat and also a/c low..

Head gasket-car began skipping and then white smoke came out of exhuast.i drove it home (3 miles).i pulled the spark plugs and found that the number 3 cylinder plug clean and wet.i did some research and found this to be a common problem with this motor and cylinder.why won't ford help?i have yet to bring it to a garage so i don't know if the head or block is damaged.i am hoping not!transmission-aod modelstarting at about 79,000 miles it began to shift funny and got progressively worse as time went on.now shifting eratic, was looking into fixing it when the head gasket problem came up!!!!!

Vehicle slipped out of park knocking consumer over and running over her ankle/leg.

Vehicle did not go into drive or reverse.the owner changed the transmission fluid and filter, which is recommended in theowner manual. Vehicle currently will not go into reverse.the dealer and manufacturer have been notified.

The brakes switch goes out,consumer loses brakes lights,no cruise control and is unable to shift from parkinto drive. The switch has been replaced (6) time since owning vehicle in july 92.

Defective tail shaft on transmission.new seal did not solve problem.mr

Vehicle slipped out of park knocking consumer over and running over her ankle/leg.

At highway speeds when making lane changes the rear end goes to the opposite of the direction it is traveling due to axle bearing failure.

Rear wheels had excessive play due to worn out bearings, causing premature wear of hubs.

Gas pedal sticking to the floor. *et

While closing driver's side door, seat belt wouldnot retract into safety position off track.motorized belt is stuck in the locked position, seatbelt does not work at all.

Automatic seat belt operation sporadic.

Driver side motorized seat belt stuck mid cycle. According to two mechanics,failure in the track system. They both report that they have had numerous complaints;in fact, the second mechanic completed my complaint after i gave him the make and mentioned seatbelts. So far, i've not had any injuries other than a bumped head, trying yo get out of the vehicle, but i do have concerns about the efficacy in an accident should the track system fail during an accident.

Automatic seat belts get stuck in the up postion.this problem occurs on the driverside. Owner is very concerned about this problem.

Upon frontal collision, both passive restraint systems failed allowing driver to hit steering wheel and passenger knees. Please describe details.tt

The doors have been a problem for quite a few years, they seem to be too heavy for the hinges as they sag and require us to lift the door to get them to shut.the front seat automatic seat belts don't work properly at all as they do not know when to retract and passenger side stays at bottom of track and shutters all the time.the parking brake pedal does not stay elevated, which causes the in-dash brake light to come on during operation.

The seat belts are motorbelts and they will will not stay in the correct position and will run up and down the track while the car is in motion.

Because of the hinges in doorit will not shut properly. Seat also will not lock .

Driver's automatic seat belt failed.

Door does not shut properly; have to lift up & then close it. The motorized seat belts do not work properly; they are not retracting backwards or fowards like they should.consumer states door hinge is not strong enough, it starts to wear after several years, dealer states that hinge can not be adjusted that it has to be replaced.

Consumer had experienced problem with active seat belt motor ondriver's side.motor won't move when openingdoor or when closing. Consumer had to be usinglap seat belt in a manual way.

I got into my car this morning and the driver power seat belt would not work. When i opened the door to my passenger sidethe power seat belt on the driver side attempted to work but didn't work completely. There was no events leading to the failure. This isn't something that has happened before. I haven't made an attempt to get it fixed yet as it just happened only a half hour ago.

The automatic seat belts don't work.on the driver's side, the seat belt stays in a position that appears to be effective, but it does not go all the way back.it also no longer moves forward when the door is opened.on the passenger side, the seat belt works most of the time.however, it occasionally gets stuck in a position where it has moved forward when the door was opened but it won't move back to its correct position.i read in the car manual that there is a knob that can be turned in order to get the seat belt to go back all the way.i've tried this many times; it worked at first, but doesn't any more.

Consumer states that driver's seat belts is inoperable, motor went out. Dealer and manufacturer notified.

No summary listed for above vehicle.

Driver side lap/shoulder belt will not retract, caught in the track and will not move backwards or forward.

Driver and passenger restraints do not retract.dealer and manufacturer have been notified.

Shoulder harness did not work. It extended to its full length.

Because of the hinges in doorit will not shut properly. Seat also will not lock .

Front seat latches failed to stop seat back from going forward in accident, resulting in injuries. *dsh

The rear brakes failed to function and no power brakes at all really hard pedal had to stand on the brake pedal to get it to stop this happened under normal driving conditions this makes it very hard to stop i was able to get it off the road called a tow truck and had it towed to my house ford.com said no recalls for my car and it cost $1500 to fix .

Electrical problem causing light to go off intermittantly while driving, consumer has had numerous switches replaced but the problem persist.

Ongoing problem with brake warning light and abs sensor lightcoming on simultaneously and intermittently, andindicating complete brake failure.dealer notified, and informedconsumer that repairs would be at consumer's cost.

When driving abs light came on and brake light came on.tried to stop vehicle and brake petal froze.please describe details.tt

While driving vehicle the abs brake pump caused the brakes to lock up without warning.owner is very concerned for safety.

While drivingbrake light illuminated, indicating a problem. Whenbrakes were appliedfront and rear brakes failed, cause unknown.please give any further details.

Abs relay malfunctioned and pump would not turn on, had no brakes.tt

Upon applying force to the brake pedal the pedal goes to the floor,causing extended stopping distace and lack of brake effectiveness, consumer has contacted the dealerand the dealer has replaced the abs assembly and the master cylinder.

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

Brake booster went out while driving 55 mph, caused total brake failure, no warning, driver coasted to a stop. Anti-lock brake module also found to be defective.

When driving abs light came on and brake light came on.tried to stop vehicle and brake petal froze.please describe details.tt

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

While driving lost braking power, abs failure.

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

While driving the vehicle the brakes totally failed.the pedal went right to the floor , there were no brakes at all.this was on normal road conditions. The system has abs.

Ongoing problem with brake warning light and abs sensor lightcoming on simultaneously and intermittently, andindicating complete brake failure.dealer notified, and informedconsumer that repairs would be at consumer's cost.

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

While the consumer tried to stop the vehicle both front and rear brakes would not grab at all, took the vehicle to the dealer and dealer told consumer the brakes had catastrophically failed. The consumer called ford factory representative and told them about the problem and admitted it was a design defect. The consumer stated that he had repeated problem with the abs system.

When trying to apply the brakes the vehicle kept on going,had to put on the emergency brake so that the vehicle could stop.

Systematic brake problems complete outages.tt

Replaced front brake rotors.

3rd set of front rotors/pads installed, after 20000 rotors warped.bad design...front rotor/calipers are too small for this car, and cause rotors to warp.

Brake discs resurfaced due to wobble and grinding noise.*skd

Brakes: brakes has beenreplaced three times within three years. Brakes vibrate and wear out within a year. Had new brake pads installed and rotors turned. Also vehicle caught fire on the left side 3-2-97. Probable cause electrical. Recall 96v071.

Brake failure, corrosion of rotors and pads are not touching, vehicle vibrates when applying brakes.tt

Brake failure, corrosion of rotors and pads are not touching the rotors, when applying brakes make a loud noise/steering wheel shakes when applying brakes.

Turned rotors.

Brake failure of the front brakes when applied vibrate, rotors and dis pads failure,

Brakes: brakes has beenreplaced three times within three years. Brakes vibrate and wear out within a year. Had new brake pads installed and rotors turned. Also vehicle caught fire on the left side 3-2-97. Probable cause electrical. Recall 96v071.

Rear brakes failed to pass inspection when using a hunter b-400 brake plate tester.*skd

Upon applying force to the brake pedal the pedal goes to the floor,causing extended stopping distace and lack of brake effectiveness, consumer has contacted the dealerand the dealer has replaced the abs assembly and the master cylinder.

The plastic transmission cable end broke off the throttle body causing the gas pedal sticking to the floor.*et

Brake pedal would not depress at all, and hand brake had no effect on slowing vehicle down, due to failed brake pump relay.

Brake warning lamp came on and driver experienced loss of brake power.

Brake booster went out while driving 55 mph, caused total brake failure, no warning, driver coasted to a stop. Anti-lock brake module also found to be defective.

The line routed from the pump to the rack and pinion was wedged inbetween the bottom of the oil pan and the top of the frame, causing it to rub through the line, wearing a hole in it. This caused it to leak p.s. Fluid rapidly. I would like to know if there was something done wrong on my part.

Power steering hose disconnected causing fluid leak on exhaust (catalytic converter) resulting in fire.

Consumer states that while driving about 5 mph , the power steering hosebecame loose,causing the vehicle to lose powersteering . The dealer has been notified.

Replaced right/left spindle.

Bumper not able to withstand minor impact, caused neck injury.

Because of the hinges in doorit will not shut properly. Seat also will not lock .

The doors have been a problem for quite a few years, they seem to be too heavy for the hinges as they sag and require us to lift the door to get them to shut.the front seat automatic seat belts don't work properly at all as they do not know when to retract and passenger side stays at bottom of track and shutters all the time.the parking brake pedal does not stay elevated, which causes the in-dash brake light to come on during operation.

Door does not shut properly; have to lift up & then close it. The motorized seat belts do not work properly; they are not retracting backwards or fowards like they should.consumer states door hinge is not strong enough, it starts to wear after several years, dealer states that hinge can not be adjusted that it has to be replaced.

Driving along at approximately 10 mph the part that turns thespindle/ lower ball joints/ lower control arm just fell off.

Ford springs i owned an escort and am on the second set of springs and just bought a 92 thunderbird and both front springs are bad this has happened to a topaz i had to what is the problem with ford and there springs lately i've been hearing a lot on this seems like when the cars get up to 75000 miles.ever heard of flats because of this problem please look into it thank you.*nlm

Drivers side rear wheel bearing/hub assembly breaking down prematurely. *dsh

I don't have the information in front of me re. Tire model, size, etc.the tread completely peeled while travelling at ~ 65 mph, resulting in extensive bumper, fender, and misc. Damage.the tire was roughly 2 years old and had less than 35,000 miles of wear.proper rotation, balancing, and inflation had been maintained.( dot number: )

Oil pressure gauge design is a phoney gauge, circuit is run through a fixed resistor which reads normal on all occasions. Mjs

No summary listed for abov evehicle.

No summary listed for above vehicle.

Ford garage unable to get part. No safety defect listed in summary.

Vehicle while accelerating car would not decelerate while driving due to stuck throttle.t

Gas pedal stuck to the floor due to throttle sensor failure.

The brakes switch goes out,consumer loses brakes lights,no cruise control and is unable to shift from parkinto drive. The switch has been replaced (6) time since owning vehicle in july 92.

Unintended acceleration, possible problem with the throttle position sensor or idle control valve.tt

Accelerator pedal sticks to floor when passing and will not release until tapped or pulled by hand.

I was driving at approximately 50-55 mph when the accelerator pedal suddenly went limp under my foot.however, the car continued accelerating.pumping the pedal changed nothing.when i took my foot off the accelerator the car kept going at 55 mph.i applied the brakes and managed to get the vehicle to stop by putting it in park while it was still moving and turning off the ignition.i was on an empty road and was able to get to the shoulder without incident.i waited a few minutes and started the car up again and it was racing at full throttle while in park.the throttle is obviously stuck wide open and i think i probably incurred transmission damage getting it to stop. I then called a tow truck which towed the vehicle to my residence.i have not yet had a mechanic look at the car.i thought i would make this report first and wait for your advice as to what to do.my guess would be the throttle cable snapped based on the fact that the pedal suddenly went limp and then i lost the ability to either accelerate or decelerate.

Gas pedal stuck to the floor due to throttle cable failure.

The orginal speedometer was replaced at 7,000 miles, the second one was replaced at 5,000 miles and the third one at 8,000 miles.please describe further details. The needle will not program past 38 mph also heater not working properly low heat and also a/c low..

While driving the vehicle the passenger's side window fell out. The window has been replaced twice, 5/95 and 8/96.

While driving consumer noticed something black falling ondash, he stopped/ inspected, and noticed a piece ofwindshield adhesive had fallen. Adhesive had never hardened,andwhen cleaning inside of it, consumer got stuck on adhesive. Ford dealer told him up to 36000 miles ford co. Would take care of this problem, but since this vehicle was over that mileage they would do nothing.consumer states problem still exists.

Consumer experiencing problems with the in windshields wipers . *et

Left wheel fell off while driving due to being loose, causing accident/injuries. *aw

Lug nut designed without safety deviceprevents lug from falling off,resulting in rear wheel coming off.*skd

Left rear wheel has become loose, due to the washer that holds the wheel on the axle is defective, replace washer 3 times.tt




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